Little update.
Took the car for a test run, the other day and all seemed fine.
But by the time I got home the engine was popping back up through the carbs a lot on the over run.
I thought it must be the exhaust and put some paste around the pipes where the slip into one another. No leaks at the head area, all nice and tight there.
When I went to tighten the clamps, one broke so I put the original style ones back on, but I over tightened one of those and stripped a thread, so then it wouldn't even come undone.
So I had to grind that nut off and re do it.
Broken old clamp
Once a got the exhaust on I went for another test drive, only this time it wasn't running well at all..... running on 3 cylinders only.
Got back and decided to look at the spark plugs, and on reaching for number one plug, I discovered the lead wasn't even attached, woo hoo ,easy fix.
Went for a test run to Weedon depot on Sunday , to see if I could see Neil Bardsley but no luck and the car was popping a little still.
So I reset all the idle screws with flow meter on top and that seems to have cured it, fingers crossed.
Karl
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